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My A/F Ratio is Crazy. Car runs weird. Help Maybe?

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  • My A/F Ratio is Crazy. Car runs weird. Help Maybe?

    Details
    98 Integra
    GSR Swap
    Bone Stock everything with a Skunk2 intake mani
    Obd2 to Obd1 Jumper
    CKF Bypass

    My car is killing gas.

    My air/fuel is all over the place.

    Ever since last week I un did my battery for a min well working on the car. When I hooked up the car it ran rich as shit. Killed gas like crazy. I thought maybe fucked up the chip inside the ecu. So I swapped tunes. Nothing. I swapped O2' sensor. Now the car runs lean. And my gauge will go all the way Lean and the car will cut out. If I hit the gas hard it will go back to rich and run normal. If I unplug the O2 sensor the car runs good. Idk whats wrong with it.

    The reason I don't think the sensor/gauge is bad, is because when it goes down to lean while driving my car cuts out. So it must be reading accurate. But thats crazy at idle. It's almost as if it's a narrow band with a autometer gauge like a fucking light show.

    I swapped...

    -Injectors
    -Fuel Pressure Regulator
    -Intake Air Temp Sensor
    -Dizzy
    -Engine Harness
    -P72 Ecu Virgin
    -P75 Ecu Virgin
    -Map Sensor
    -TPS
    -Throttle Body
    -3 differ O2 sensors

    All the parts I swapped. I swapped with parts I knew worked.

    Checked for vaccum leaks. Nothing.
    My vaccum reads good.
    Nothing same shit.

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    Money ain't a thing! Crew Member #1

    Stock LS Papa!

  • #2
    ttt
    Money ain't a thing! Crew Member #1

    Stock LS Papa!

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    • #3
      It's fucked, bad valve smfh
      Honda sucks. Over priced junk.

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      • #4
        nope. doesn't misfire. it ran out of gas on my way home lastnight. On the road into my neigborhood. I rolled down to my drive way. Just couldn't make it in the drive way. Well. I hope it ran out of gas. If not then something else is wrong lol. I went out a lil bit ago and primed it over n over n it wouldn't start.
        Money ain't a thing! Crew Member #1

        Stock LS Papa!

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        • #5
          something doesn't seem right with the transition between closed/open loop. did anything ground out when you had the battery disconnected? what else changed from unplugging the battery, to reconnecting it? anything?
          590852836f5fbce940_b
          In Loving Memory of Nick "NHSwaps13203" Haines

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          • #6
            did u try disabling the o2 and iat in crome yet? its weird becuz it jumps around then goes optimal then lean then rich then lean etc..

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            • #7
              Originally posted by AWDream View Post
              something doesn't seem right with the transition between closed/open loop. did anything ground out when you had the battery disconnected? what else changed from unplugging the battery, to reconnecting it? anything?
              I reset the battery before with no problems. And after this problem started i've prolly reset the battery 50 times lol. And nothing grounded out at the time when I did it.

              Originally posted by mark11017 View Post
              did u try disabling the o2 and iat in crome yet? its weird becuz it jumps around then goes optimal then lean then rich then lean etc..
              Did that! Still ran like a crack head on steriods.
              Money ain't a thing! Crew Member #1

              Stock LS Papa!

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              • #8
                idkk if you unplug the o2 and it runs fine then ???

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                • #9
                  not fine. but better then when it's plugged in.
                  Money ain't a thing! Crew Member #1

                  Stock LS Papa!

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                  • #10
                    bring it to vtecboost i guess thats ur only option

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                    • #11
                      Retune?
                      Money ain't a thing! Crew Member #2

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                      • #12
                        Originally posted by mark11017 View Post
                        bring it to vtecboost i guess thats ur only option
                        lmfaoo


                        Originally posted by LS/Vtec
                        why yu mad doe

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                        • #13
                          Originally posted by egkid129 View Post
                          Retune?
                          tried 3 differ ecu's. I put the car to boneeeee stock. To eliminate any problems. Minus the skunk2 mani. Idk doesnt make sense.
                          Money ain't a thing! Crew Member #1

                          Stock LS Papa!

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                          • #14
                            Still boosted?
                            Money ain't a thing! Crew Member #2

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                            • #15
                              Nope. Put here to 100% stock. Tyring to figure this problem out without wondering if it's other things causing it. So It's all stock with a skunk2 intake mani. I'm not trying to put the stock one back on lol
                              Money ain't a thing! Crew Member #1

                              Stock LS Papa!

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